| The Everyday Practicalities of Heating and Powering your Home - using renewable Fuels. |
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| As Inspiration: A 1938 Lister CS direct drive generator - a DC Battery Charging Set. |
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| This page documents ideas, jottings and performance figures as they occur, so as to serve as a lab notebook and a record of proceedings. Sorry for lack of photos - see earlier pages for pictures of the system components. Having assembled the system, there was now the task of getting the it to work reliably and conveniently, and to interface efficiently with the household electrical and heating systems, so making an appreciable contribution to offsetting my grid power and natural gas usage. Some questions were: 1. How much power is available and at what overall efficiency? 2. How long will the fully charged battery bank keep the office and other light loads running? 3. How much fuel is needed to recharge the batteries after a typical overnight battery run? 4. How much heat can usefully be extracted from the system? 5. How best to integrate this heat content into the central heating and DHW requirements of the house? 6. How to assess the overall performance of the system, in terms of electricity and gas saved? 7. A documentation of any operational problems. Some System Objectives. The Lister CHP system should be able to do the following: 1. Provide 4 to 5kW of heating for the radiators, underfloor heating loop and heat the 120 litre domestic hot water cylinder. 2. Supply 1700W of electrical power for a 12kWh electric storage heater for office heating. 3. Provide up to 2500W of electrical power for powering the office, washing machine, dishwasher etc. 4. Provide up to 8kWh per day to offset grid electricity usage, and provide overnight battery back-up. |
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| Friday September 21st 2007. Following some recent installation work of plumbing and cables, renewable heat and power has now been brought into my household. I am using my office area as a guinea-pig, mainly because it is under my control, more often than not occupied, I use between 2 to 4 kWh of electricity each day, and I have a fairly constant need for background heat during the winter months. The Lister recharges a battery bank to a nominal 125V dc and this is used to power a large inverter consisting of two 2500W units. They can be used in isolation or ganged together to make a 5kW inverter. The output of one inverter is brought up to my office via a 25m length of 2.5mm2 cable. This terminates in a double switched 13A socket, one half is used for the 1700W storage heater and the other feeds the rest of the office equipment, which may be up to a 400W load. Further cables will be brought in to supply selected loads such as the dishwasher, washing machine and probably the kettle - as these represent most of our high wattage appliances. The inverter is consuming 121.8V at 18.9A from the batteries = 2290W The storage heater, office equipment and engine room light amount to 1645+ 215 +60 = 1920W So the inverter is operating at about 83.85% efficiency. The current flowing into the batteries is measured on an oscilloscope and is pictured below. Generator current = 19.8A x 121.8V = 2412W The hot water output is 50 litres per hour at 24.2 C temperature rise - so about 1.4 kW. Improved pipework and better insulation would improve this considerably. 13:00 Engine started 13:04 Storage Heater turned on 14:52 Office supply switched over to inverter 16:29 Storage Heater Turned off On Time 3 hours 25 minutes KWh used 5.62 Mean Power 1645 W |
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| Here is the current waveform as measured by a current clamp meter connected to a Fluke digital Scopemeter. The current here is measured by the millivolt reading so +19.8mV is equal to 19.8A flowing into the battery from the dc generator. The frequency reading 5.411Hz should be multiplied by 120 to give rpm - in this case 649.32rpm. Note the distinct peak in the waveform for the power stroke and the lesser peaks for the exhaust and induction strokes. The trough in the waveform is of course the compression stroke in which kinetic energy from the flywheel is being used to compress the air charge. With heavier flywheels, such as on a Startomatic, the peaks and troughs would be less pronounced. |
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| Temperature Measurements. Initial Run Friday Sept 21st 2007. Outside temperature 17.7 C After 3 hours running Top of Local Store 92.6 C Engine coolant inlet 64C Engine Coolant Out 94 C Top of DHW Tank 62.2 C Bottom of DHW Tank 45.9C Tank start temperature Top 35C, base 22.8C Energy in DHW tank Exhaust Heat exchanger inlet 39.5 C Exhaust Heat Exchanger Outlet 75.5 Flow Rate 50.4 litres per hour Heat exchanger power = 2.108 kW Heat exchanger and exhaust need properly insulating. Energy into storage heater in 3hrs 25 mins = 5.62kWh = 1.645kW power Energy into office in 2hrs 54 minutes = 0.78kWh = 200W power Engine room fluorescent light = 60W Total power = 1905W Fuel Burn Rate (at 9.4kWh/litre) =10.575kW Conversion Efficiency from veg oil to ac power = (1.905/10.575) = 18.01% Fuel Used: 3 litres in 2hrs 40 minutes. = 1125cc per hour |
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| About two thirds of the heat energy contained in the fuel will be rejected from the engine, in the coolant circuit and the exhaust. For best overall system efficiency, the CHP system needs to capture as much of this heat as possible and make it available in a form that is directly useful for the property to be heated. Because of system pipework temperature limitations, the heated water should not exceed 90 centigrade. The coolant in the engine should also be limited to around 90C. My first approach was to plumb in a local gravity feed store to provide engine cooling, and to moderate the peak system temperatures. Sizing of this store, and the rate at which heat is extracted appear to be critical to the efficiency and heat-up time of the system. Following the initial 3.5 hour run, the local tank had reached 92.6C and the DHW cylinder was receiving water at 65 centigrade. To get a better idea of the thermal performance, we can consider the engine coolant circuit to approximate a 2kW heater, and the exhaust heat exchanger also a 2kW heater. |
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| Saturday 22nd September 2007 . Weather sunny spells warm Overnight the battery terminal voltage has dropped to 106.0V powering the office. Decided to run the engine on just 3 litres of fuel as a typical battery recharge cycle. 10:00 The empty fuel tank had 3.0 litres of filtered WVO added 10:00 Engine started on high compression 116V at 27.4 A battery charge current 3178W 10:10 Compression setting lowered 10:40 Engine stopped due to defective pipe joint flooding workshop! 1hr 50 minute shut down. 12:30 Engine restarted - high compression 12:40 Compression setting lowered 13:07 Battery Voltage 121.9V, charge current 17.7A 2157.6W 13:30 Battery Voltage 122.6V, charge current 14.3A 1753W 14:00 Battery Voltage 122.4V, charge current 10.3A 1260W 14:00 Water from house 27.7C, return to house 56.6 C (washing machine drawing from hot) 14:30 Rapid drop in battery charge current 124.6V @ 8.0A 996.8W 14:30 Engine shut down. Fuel used 2.8litres Fuel remaining <200ml Run time 2 hrs 40 minutes, fuel used 2.8 litres. Average fuel consumption 1050ml per hour As can be seen, the charge current on the batteries is rapidly decreasing as they charge up. This was most notable in the last half hour of the recharge. The load on the engine decreases and this is why it may be beneficial to use the storage heater or other domestic loads to help maintain a more constant load on the engine. |
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| Sunday 23rd September 2007. Weather Warm, Sunny spells 21 C The Lister CHP system produced enough hot water last night for us both to enjoy hot baths - I much needed one having been splattered with engine oil and prematurely showered with water earlier in the day. The engine was shut down at 2:30pm and the office continued to run from the batteries and inverter. Overnight the office was semi-powered so continued to draw about 100W. At 8am this morning the energy meter showed that I had used 6.73kWh of power in the office in the last 42 hours since 3pm on Friday afternoon, plus 5.62kWh were used in the electric storage heater on Friday. Checking my daily energy figures, my gas consumption showed a significant drop for the last 3 days, and the electricity was also down by about 2.5 KWh per day. By 9am the battery bank voltage had dropped to 99.0V, and with a recommended minimum of 10.8V per battery (97.2V), it was decided to restart the engine and give the batteries their daily charge. Batteries follow a very distinct charging curve. They start off drawing a high current and this then tapers off until the battery is fully charged and drawing very little current. I took voltage and current readings every half hour to illustrate this charging behaviour. This means that the engine begins the recharge cycle on a high load of about 3.2kW which tapers down to 900W when the batteries are near charged. 11:00 am Office active at about 330W consumption - 2 x PC, router etc. 11:00 7.4kWh consumed in 44 hours - mean office consumption of 168W 11:30 Engine shut down - run time 2.5 hours - fuel used 2.6 litres Average fuel usage 1.04 litres per hour. System Efficiency During the 2.5 hour battery charging cycle, the generator was producing an average of 2.25kW. So the approximate total electrical energy into the batteries = (2.5 x 2.25) = 5.625kWh The energy content of the fuel burned = (2.6 litres x 9.4kWh) = 24.44kWh So the average conversion efficiency of veg oil to dc into the battery = (5.625/24.44) =23.01% The heat recovered into the 120 litre DHW tank can be estimated from the tank start temperature and the end temperature. Note that the top of the hot water cylinder may well be 20C hotter than the base. From the temperature measurements taken, the heat captured into the cylinder is about 2.9kWh. This is a fairly poor result, and reflects the low flow rates, the heat losses and the inefficiency of the existing pipework. |
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| Monday 24th September 2007. Battery voltage was down to 96V at 8am this morning suggesting that a full recharge was in order. 08:00 Engine started with 3.4 litres in tank 10:00 3 litres of WVO added 10:00 Dishwasher started 10:20 Dishwasher commences heat cycle 10:25 Generator 109.7V @ 20.6A Inverter 109.7V @28.5A 11:45 Dishwasher stops after 1.43kWh consumed 11:52 Washing machine started 12:10 1.75l of fuel remaining 12:45 Engine shut down 14:00 Washing machine started for second wash - 1.19kWh consumed 18:00 Office consumption 8am to 6pm = 1.7kWh Running the dishwasher and then the washing machine (twice) from the inverter had proven successful. As of 6pm the rest of the house had only consumed 2.0kWh in 10hrs since 8am and with 4.32kWh offset from the grid onto the veg oil generator. |
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| Tuesday 25th September. Chilly, bright start, with clear skies last night. Central heating fired about twice in the night. Purchased 6 way split RCD protected consumer unit and MCBs to be installed on the inverter output. Engine started at 09:15 with 3 litres of fuel added to tank. Batteries had got low, although terminal voltage still showed good state of charge. Tripped out the Battery Low volts at 93V when trying to boil a kettle at 2.7kW. Inverter restarted at 09:30 Batteries will need an equalisation charge about 2 times per week in order to keep them up to full capacity. Now pressing need to plumb the output of the Lister into the DCH, in order to allow longer runs and shift some of the waste heat. New Fuel tank with Burette level indicator planned. 11:45 Generator shut down because of suspected bearing failure in dc starter/generator or ST alt. Fuel remaining 1.5 litres Motor casing feels very hot, and there is a general graunchiness about the belt drive. Fortunately I have a spare motor which could quite easily be swapped in but - this will give me something to fix! Evening Update. Stripped out the PM dc motor/generator to find that it was almost entirely seized. Either a bearing has failed, or the rotor is now touching the stator and putting a whole lot of extra friction on the shaft. Got the new motor into place, aligned the shafts correctly and ensured that the belt was not over tightened. 20:15. With remaining fuel - about a litre, ran the engine for 45 minutes in order togive the battery a much needed charge. With these home built systems, there is a fair degree of flexability on what can be done, with improved system components available from time to time. |
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| Wednesday 26th September 2007. Added 3.0 litres to the now empty fuel tank. 17:25 Engine started for battery charging. 18:25 Engine working hard, 30.5A at 119.5V into batteries. (3645W). 1.5 litres fuel remaining 18:25 DC motor warming up - but not critical. Belt tension OK 19:25 End of charge period, 125V at 25A (3125W). Engine shutdown. Engine almost out of fuel. 19:30 3 litres of fuel added for tomorrow. This was a fairly high powered run, with the engine working at full load, into quite exhausted batteries (93.5V the inverter cuts out on low battery volts). 3 litres of fuel consumed in just 2 hours. The engine maintained an average of about 3500W into the batteries for 2 hours - so about 6 or 7kWh returned. Lots of hot water too. I am going to re-instate the 3kW ST alternator as an alternative means of extracting power from the system. After a 2 hour battery charging run, the alternator can be energised by turning on its field coils and contribute say 1700W of power to the upstairs storage heater. This will take some of the load of the dc generator and give it a chance to cool down. No more seized bearings I hope. |
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| Thursday 27th September. Rebuilt the motor mount this evening to correct the problems of shaft alignment and belt tension. The 3 motor mount bolts that hold the mounting plate down onto the original Startomatic slotted rails were turning. Replaced these bolts with M12 x 40mm, bolting down into a rectangular captive nut, that fitted nicely into the slotted rail. Motor alignment corrected to make it parallel to the ST alternator and belt correctly tensioned. 3 litres of fuel in tank 18:15 Engine started for battery recharge. 20:00 Additional 3 litres added to tank 21:00 Dish washer started using the feed from the ST alternator 22:45 Dishwasher cycle stopped. 1.50 kWh consumed. Engine shut down -almost out of fuel. Fuel Used - 6 litres Time of engine run : 4 hours 30 minutes Office consumption at 11pm: 3.40kWh Hot water from engine reached 78 C. Tickling an ST alternator into Life. The ST alternator relies on residual field remaining in the soft iron rotor core to allow it to self excite. Unfortunately this might not happen, even though the alternator is spinning at 1500rpm with the Lister at it's rated speed of 650rpm. Only an engine overspeed can coax the ST into self exciting. The solution to this is to apply an external dc supply to the field winding - by connecting across the slip-ring brush holders. Note the polarity of this connection, by first testing the voltage across the slip-rings with a DVM. I clipped a couple of small croc-clip leads onto the brush holders and applied 12V dc from a battery charger. Immediately the ST comes to life. The next time this happened, the battery charge was not to hand, so I reached for a somewhat dead PP3 battery and used this. Even the 6V remaining in the PP3 was enough to excite the field sufficiently to get the ST to "fire-up". I am going to build a small rechargeable battery into the ST, and a switch circuit which will allow me to manually excite the field. With the ST running at rated speed, there is about 24 to 25V measured across the brushes. The resistance of the rotor is in the order of 2 ohms, so the field current is about 1.25A. This source of low voltage dc could be used to trickle charge a rechargeable battery - not only for field excitation, but possibly for powering the engine monitoring system. Notes about heat output The generator set is providing considerable waste heat, particularly when run for longer than a couple of hours. Part of the improvements planned will be to get efficient utilisation of this waste heat. At the moment it is contributing to my domestic hot water supply, with 3 litres of oil supplying sufficient waste heat to heat the 120 litre hot water cylinder to 55C, and heat up the engine "local store" to around 95C. After the recent 4.5 hour run, the water returned to the house was at 78C, in spite of the uninsulated heat exchanger and poorly lagged local store tank. Clearly there is a considerable amount of waste heat available, and it just needs to be captured and used more effectively. My existing heating system has the circulating pump fitted in the boiler flow, where it then is split via the 2-port electric valves into separate flows for the radiators and the domestic hot water. The intention is to T the flow from the Lister circulation pump, into this pumped flow, using non return valves to prevent the heated water from one source, back-flowing through the idle pump of the other source - i.e. either shorting through the boiler, or back feeding hot water through the Lister system. |
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| Friday 28th September 2007. Always make a point of turning on the circulation pump BEFORE you start the engine! 5 minutes of heavy load running, without circulating water will boil the water in the exhaust gas heat exchanger! 10:00 3 litres of WVO fuel added into nearly empty tank. 10:05 Engine started and ST alternator tickled into action. 10:10 Circulation pump turned on! Engine set to low compression 10:15 Washing machine plugged into output from ST and put on pre-wash cycle 10:30 Battery voltage 127.5 V charge current = 20A 10:45 Washing machine appears to be working normally. 11:00 Batteries charging at 128.6V at 18.7A 12:35 Engine shut down, 100ml fuel left. Battery Voltage 132V at 13.5A 12:35 Washing machine and office continue to run on battery/inverter supply. The dc output from the generator appears to be able to charge the batteries at fairly high currents - right up to the float voltage and above. Whilst the dc generator might be a good way to get a lot of charge into the battery bank in a short time, it may be overcharging the batteries at the end of their charge cycle. A mosfet speed/charge controller will be needed for the dc starter generator, so that it can keep the batteries floated at a smaller current. As there are 4 parallel stings - even 20A is divided into 5 amps per string. Enersys recommends that batteries are given a freshening charge of 2.27 to 2.4 volts per cell, and at a current of 10% of C10, for 24 hours. http://www.enersysreservepower.com/documents/PS-SBS-CL-IS-UN-v2.pdf So for my 54 cell string, a charge voltage of 129.6V is acceptable. The SBS 40 battery has a quoted C10 capacity of 37Ah to a voltage of 1.8V per cell. This suggests that 3.7A per string is acceptable for a refresher charge - therefore 14.8A for the combined current of the 4 parallel strings. Weekly Summary. 31 Litres of WVO consumed 32 kWh of power utilised in the house. * * This is an estimate because I had 3 energy meters plugged into various circuits, and a couple of them reset losing their current total KWh reading. New electricity meter to be installed at the weekend - should solve this problem. |
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| Saturday 29th Septmber 2007. An early start and drove down to Devon to visit some renewable energy colleagues. Nigel has a large house in Devon, where he has installed a 1kW solar pV array and a 2kW Navitron wind generator. Although sunny, the wind turbine failed to produce any power. He charges up a 48V battery bank - salvaged from an old fork lift truck battery. When the wind don't blow and the sun don't shine, he has a little 2 cylinder Kubota engine generator that he runs on solid vegetable oil - often commonly referred to as lard. The waste heat from the Kubota engine supplies the heat needed to melt the lard. The excess will be used to help heat the house and the hot water tank. A 7kW Studer inverter converts the dc from the fork-lift battery bank to ac to power the house. We spent the afternoon welding up a new frame to accept the engine and twin truck alternators. |
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| Sunday 30th September 2007. Saturday was spent in Somerset and Devon, so today I got home early and decided to have a day spent working on the wiring and fuse board in the workshop. 07:00 Left Taunton 09:15 Arrived Redhill, Surrey. Spent the morning making the enclosure for the workshop wiring and engine control system out of an old packing case that once held a 5kW ST alternator - perfect size for the job. Made up "Fuse board" from spare kitchen unit back panel, and fitted the 6-way "Contactum" consumer unit and the Iskra digital electricity meter that has a 1 Wh pulse output. I now have 6 circuits with individual MCBs and RCD protection for the workshop power. Dishwasher 16A Washing machine 16A Living room double socket 16A Office double socket 16A Workshop sockets 10A Workshop lights 6A 18:30 3 litres of fuel added to Lister fuel tank and engine started 21:00 Engine shutdown after 150 minutes runtime - about 0.5 litre fuel remaining. 22:00 Circulation pump turned off. Runtime 150 minutes - fuel use - about 2.5 litres. |
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| There was a useful space above the inverter cabinet, so I cut down a 5kW ST alternator packing case, which was a perfect fit, to make a custom enclosure for the fuse board and the electric meter and associated wiring. Eventually this will be expanded to house the engine monitoring and control system and the grid change-over switch. Just above the white uPVC window, is the 40mm white trunking that carries the 4 circuits back to the house - washing machine, dishwasher, office and living room - all are terminated in double sockets. |
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| Shot of the "Fuse Board" This was the back panel of a kitchen unit that was surplus after the kitchen installation. 700 wide x 500 high. I took advantage of the mid-day sunshine to wire up the 6-way consumer unit and the Iskra import-export electricity meter. The meter tails are 6mm2. My inverter is only rated at 5kW, so 6mm2 is perfectly adequate for short runs. |
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| The meter and consumer unit, now populated with the MCBs was put into place above the inverter cabinet. It hinges forwards on the bottom screws to allow the wiring to be accessed from behind. The blue panel below is a digital meter showing the inverter battery volts and amps as well as a load of warning LEDs that I usually try to ignore. |
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| With all the MCBs wired up from behind the front panel was screwed into position and the system tested. Perhaps the lack of smoke and sparks suggested all was well with my installation. I have been wiring plugs since the age of 5, and all electrical installation work is done at my own risk. Part P - Eat your heart out! |
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| A close-up shot of the Iskra meter - bought for £35 on Ebay. This is an import export meter, and gives one flash of the LED for every watt-hour consumed. It also has volts-free pulse outputs for both the import and export - which will be very easy to interface with my data logging unit. One flash per Wh consumed. |
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| The Contactum 6-way split consumer unit. 4 of the circuits are protected by 16A MCBs whilst the lighting circuit and ring main in the workshop have RCD protection. |
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| Monday 1st October 2007. 08:30 3 litres of fuel added - engine started 08:35 Low compression, dishwasher started 10:30 Dishwasher cycle ends, 1.43kWh. Engine stopped. Fuel Usage Approx 2.5 litres Run time 120 minutes. The new meter on the inverter output shows that 2.0kWh have been consumed by the dishwasher and the office since 08:00. The household continued to run off the inverter for the remainder of the day, and I arranged that the water circulation pump (54W) and the TV/Video stack was also benefiting from Lister power. |
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| Tuesday October 2nd 2007. The inverter battery voltage had fallen to 100.0V by 8:00am this morning. Whilst this is not critical, it is a good point to re-start the generator and recharge the batteries. This was now becoming fairly routine, start the engine first thing in the morning to recharge the losses in the batteries incurred during the last 22 hours. Once the batteries have picked up a little charge, make use of the power available to run the high wattage appliances such as the dishwasher or washing machine. The new electricity meter showed that a total of 7.8kW had been supplied to the house in the last 2 days from the inverter, 6kWh of it used on Monday alone. An Electrisave power meter has been fitted to the output tail of the inverter. It has a wireless link up to a display in the office, so I can glance over and see how much power is being drawn from the inverter. With just the office, it hovers about 380 to 400W, rising to 2520W when the dishwasher is heating its water. 08:00 3 litres of fuel was added to the tank and the engine restarted. 08:45 Dishwasher cycle started 09:00 Dishwater heater comes on. Lister gen working hard. Vols and amps readings follow: Generator output = 33.3A at 112.6V = 3750W. Inverter input power = 26.6A at 112.6V = 2995.6W Power to house =2.52 kW Inverter efficiency = 84.1% Overall efficiency (generator to ac outlet) = 67.2% 10:30 Engine shut down 18:10 3 litres fuel added. Engine started 18:40 Engine shutdown. 23:50 Battery Volts 105.5V. Total kWh used from inverter =12.8 Total run time today 180 minutes Wednesday 3rd October 2007. Inverter meter reading = 12.9 kWh . So 5.1kWh used on Tuesday 08:00 Battery Volts 102.4V. 08:05 About 2 litres fuel remaining. Engine started for battery charging 09:15 Batteries up to 123.0V, still charging at 26.5A. Engine shut down. Run time 70 minutes The short 30 minute run yesterday evening and the run this morning are not efficient use of fuel, with the 3 litres of fuel consumed in just 100 minutes. Longer runs will be preferable particularly when the heat can be better utilised. Overnight inverter power is very inefficient use of the inverter which draws a fixed load of 200W, so a total 1.6kWh drawn from the battery for the 8 hour period, just to supply 0.1kWh. What's needed is a more efficient low power inverter that can run in sync with the big one, and supply perhaps a maximum of 1500W, but at a much higher efficiency. As it would happen, my mate Simon had found a 1500W computer UPS system in a scrapyard with two external battery packs. £ 30 secured the deal. With a 96V battery voltage, it was close to compatibility with my 108V system and used much less standing current than the old lighting inverter. During a 10 hour recharge period overnight it consumed 0.7kWh. By 11pm battery voltage was getting dangerously close to the low voltage cut off point of the inverter. The inverter was switched to standby mode where it draws about 30 to 40 W from the battery. The inverter will not boot-up until it sees a health battery voltage of at least 117V, but will continue running down to 93.5V. It can be switched back to idle any where between these two voltages (or >117V) and then be re-enabled. This gives the option of turning the big inverter to idle at say 100V overnight and then running the night time load from the small inverter. |
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| Thursday 4th October 2007 The battery pack had got very low overnight. I decided to run the engine for at least 2 hours to recharge the batteries, and then keep it running whilst the dishwasher went through its wash cycle. 09:00 3 litres fuel added. Generator started 10:00 Battery volts = 117V, inverter started. Office load switched over to inverter power. 11:00 Fuel nearly finished. Another 3 litres added. Dishwasher started 13:30 Engine shut down. 400ml fuel remaining. Run time 270 minutes. Fuel used approx, 5.6 litres. |
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| Friday 5th October 2007. The 1500W inverter has been powered up for 33 hours and drawn 3.08kWh from the mains input. This suggests that it has a quiescent power consumption of about 93W. I am considering the best approach to using it within the system. Because of its low quiescent consumption, it could be argued that it is wired directly to the grid and powers the essential circuits in UPS mode up to a maximum of 1500W. If Lister power is available from the ST alternator, then this could be fed to the ac input of the UPS, via a change over switch. ST power could also be used directly for running the storage heater in the office and any other resistive heating devices. The UPS inverter will happily handle the interruption to supply during change over, and if a white meter were available, recharging the UPS could be arranged to occur at night so as to benefit from the lower rate tariff. The UPS would ensure that essential loads such as the fridge/freezer, VCR clock, lights and office supply were maintained and supplied predominately from the Lister generated power. The Best Power 610 Inverter claims an ac to ac efficiency of 83%. Fridge & Freezer 0.75kWh Lighting 0.5kWh Office 3.0kWh TV/Video stack 0.5kWh Total 4.75kWh per day The battery back-up is about 3.5kWh so with a little experimentation the UPS should be able run these systems for about 18 hours. |
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| Saturday October 6th 2007. The workshop project is making good progress. Most of the electrical wiring is in place and on Friday afternoon, I moved the door frame for the engine shed door, into its final position, and reversed the door in the frame, so it makes it impossible to accidently walk into the Lister when its running. My nephew Adam came up from Southampton to stay this weekend, and together we cleared out the engine shed and got ready for the concreting of the Startomatic mounting base and the foundations for the forge area, expected for next Saturday. Behind the engine shed will be a substantial concreted apron for storage of the 1000 litre veg oil IBC and the fire wood for the wood-burning boiler. The Startomatic engine will sit on a block of concrete, 1200 x 900 x 450mm isolated from the rest of the shed. With the work proceeding, it was 4pm before we got a chance to run the engine. 16:00 Added 3 litres fuel. 17:00 Started up dishwasher 17:50 Out of fuel - added 3 more litres 19:00 Shut down engine. 180 minutes runtime, estimated 5 litres fuel used. |
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| Sunday 7th October 2007 Continued to work on workshop with Adam. Extra shelves were added to the benches in the workshop and a set of 5 substantial shelves made from some old chipboard panels. Dug the trench across to the "garden office" so that heating pipes and power cables etc can be routed across. Continued to work on the groundwork that has to be done prior to laying the concrete out at the back. The engine shed will be extended at the back with a 1200mm x 3000mm lean to which will provide storage for the vegetable oil IBC tank and the supply of firewood. Below are some of the pictures showing progress over the weekend. |
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The Lister engine is situated behind the partition wall between the engine shed and the workshop. Next to the Lister is the salmon pink coloured "Plint" dynamometer. On Saturday, we will be laying some more concrete to complete the engine shed floor, and to lay a 120 sq ft apron of concrete between the engine shed and the "garden office". |
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| The "engine shed" is a 10' x 10' space intended to house the two Lister engines, the dynamometer and the metal working forge area. With the doorframe repositioned on Friday, he remaining plywood wall panels were fitted with the 75mm of thermal insulation installed in the gap. The Lister is run on a daily basis for a couple of hours to recharge the large battery bank situated in the workshop next door. |
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| Here we see the view looking into the 10' wide engine shed from the open end. In order to move some of the large equipment out of the shed it was easier to remove the wooden panels from the back wall, than manoeuvre them through the door. Here the engine crane is shown supporting he spare Startomatic baseplate, ready for the installation of the Startomatic when we get the mounting block of concrete laid. |
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| The engine shed has been tidied out to allow access for concreting next weekend. The floor will be extended by 910mm to allow the forge area to be constructed. The forge is a 1200mm wide brick built fireplace and chimney allowing space to install the woodstove and the experimental gasifier. This shot shows the start of the digging for the substantial concrete block to take the Startomatic generator engine, a block of concrete 1200 x 900 x 450mm, about 1100kgs of concrete. |
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| Monday 8th October 2007 I have taken to shutting down the large inverter at night in order to maintain battery capacity. When idling it draws 30 to 40W as opposed to the 200W when running. The inverter can be switched from run to idle with a single pole switch. It is anticipated that this will be done remotely or under microcontroller control using a relay. 08:00 3 litres of fuel added to 0.5l remaining in tank 08:20 Engine started 08:30 Dishwasher started 09:50 3 litres fuel added 11:30 Engine shut down. Run time 190 minutes. Fuel used 3.8 litres The Lister has now consumed 61.3 litres of fuel since Friday 21st September. The total run duration has been 2840 minutes and 61.24kWh of power consumed from the inverter. Since fitting the electronic meter on the inverter output, 30.2 litres of veg oil burned and 30.6kWh of power consumed - plus a fully charged battery bank. This appears to be setting the baseline for consumption. Allow 1 litre of WVO per kWh electricity consumed and 1 litre will last 45 minutes typical runtime. |
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| Tuesday October 9th 2007. With 2 computers active in the office yesterday and the dishwasher, the total consumption from the inverter was 3.7kWh. I have continued to monitor my grid power usage and have noted that the sum of my grid power plus the inverter power is greater than what I was using from the grid alone 3 weeks ago. I am actually becoming wasteful of power - because I have it available from the Lister! This situation will definitely need further investigation. I keep a running total of the gas and electricity consumption figures for the last 365 days. This show the long term trend of whether I am consuming more or less energy. The figures for the last 365 days are: Gas 12224 kWh Electricity 2473 kWh Looking at the latest consumption figures, it would appear that I can generate all my electricity for just short of 2500 litres of filtered WVO per year. This corresponds to 2 1/2 IBC containers over the course of the year. The other point to note, is that the gas usage to electricity usage is in the ratio of 4.94:1 - approximately 5:1. I am currently spending £768 per year on electricity and gas, so in theory this could be reallocated to purchasing filtered waste vegetable oil in 1000 litre IBCs. The big question is can I get the balance between heat and power such that I can use the Lister generator set throughout the year. With about 5kWh of recoverable heat, for every unit of electricity consumed, and roughly 7 units of electricity used each day, there will be the problem of what do I do with 35kWh of waste heat in the summer - perhaps I should be buying a hot-tub? In Spring and Autumn, that waste heat will help keep the house comfortable, and in mid-winter, I will be producing extra electricity to run a couple of storage heaters. It is starting to become quite a complex problem of energy management, to utilise efficiently what is available without creating an excess or unnecessary burning of fuel. It might be worthwhile investing in some additional batteries so that the 1500W inverter has its own large 96V battery bank. A 300 litre thermal store is also in the planning stage. The following readings show how the generator becomes more lightly loaded as the battery voltage rises. 08:00 3 litres fuel added. Engine started, Power into batteries = 120V at 30A = 3600W 08:30 Generator producing 124.0V dc at 25A (3100W) 09:00 Generator producing 127.5V dc at 20A (2550W) 09:30 Generator producing 130.0V dc at 16A (2080W) Washing machine started on 90 minute cycle. 10:00 Generator producing 132.2V dc at 16A (2112W). Battery refresher charge. 10:15 Dishwasher started on 90 minute 65C wash cycle. This should improve the load balancing! 10:30 910W being consumed from inverter - measured on Electrisave 10:35 Dishwasher heating element kicks in - 3.05 kW from inverter. 11:50 Dishwasher finishes 12:00 Engine shut down Run time 240 minutes. Estimated fuel used 5 litres. |
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| Wednesday 10th October 2007. In the last 20 days, I have used 71kWh from the inverter and 96kWh from the grid. The average daily runtime, on days that the engine is run, is 181 minutes. With the weather cooling, it is now time to step things up a gear, and run the engine longer. Rather than the typical 3 hour run, it will soon be time to aim for an 7 or 8 hour run, and consume about 9 litres of fuel per day. This should allow a complete move away from grid power, and a large percentage of the gas consumption offset to CHP heating. To achieve this, the plumbing will have to be altered to allow for a greater heat dissipation within the house, by utilising the central heating loop and the underfloor heating as well as the domestic hot water. From an electrical point of view, either additional battery storage capacity will be needed, to absorb the additional power, or it will be consumed in water heating or storage heaters. 19:00 3 litres fuel added. Engine started. 21:30 Engine shut down Run time 150 minutes. |
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| Thursday 11th October 2007. I have been preparing the area behind the engine shed for concrete which is arriving on Saturday morning about 10am. Behind the shed will be a concrete area about 4.5m x 2m, suitable hard standing for all the heavy items not needed in the shed. The hard standing will be roofed over to form a lean-to shelter. Tomorrow I hope to install the pipes and cable ducts in a trench under this area, which convey the heat and power from the engine shed to the garden office. There will also be a drain and soak-away for the salvaged stainless steel sink unit which will be installed in this lean-to. The sink unit will allow oily and dirty hands to be washed outdoors next to the workshop, with hot water without having to return to the kitchen. 18:30 3 Litres fuel added. Engine Started. Dishwasher started 20:30 Engine shutdown. Runtime 120 minutes. |
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| Friday 12th October 2007. Much of today was spent digging the pit for the new Startomatic mounting block. Concrete is due tomorrow morning. See this page for details. |
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| Saturday 13th October 2007. Concrete arrived about 9:45am, and the morning was spent laying it. In the afternoon, Paul, my Startomatic friend turned up with a couple of very large steel expansion vessels, that had been salvaged from a commercial buildings heating system. One was 200 litres and the other is 300 litres, they will make excellent thermal stores or the smaller as an oil tank for the Lister. 18:30 Lister started for quick battery top-up charge. 19:00 Lister shut down |
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| Sunday 14th October 2007 Today the Startomatic engine was installed on its base. See this page for details. |
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| Tuesday 16th October 2007 This evening the Startomatic was rigged up with a temporary exhaust and fuel tank and given a first test run. The massive flywheels make hand-cranking much easier than on the standard 6/1 engine and withing a few turns it had fired and was rapidly gaining speed. The temporary exhaust was very loud and there was a great deal of sooty black smoke, suggesting excess fuel or a dripping injector. I will get the proper exhaust and water cooling arranged and then she can be given a proper test run. |
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| Wednesday 17th October 2007. Using my digital voltmeter I confirmed that the Startomatic alternator was indeed producing ac power. The regulator will need adjusting because I was measuring 280Vac at 60Hz and the engine was still accelerating. The engine fuel rack was quickly shut down to bring the speed down from a scary 780rpm, and took about a minute to come to a complete stop. |
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| Thursday 18th October 2007. The colder weather is finally upon us. Last night was probably the coldest so far this Autumn. At 8am the outside temperature was a chilly 4.5 degrees C. In side the engine shed, which currently has no back panel, it was 5.5C and in the insulated workshop it was 9.2C. With the Startomatic installation taking up much of the spare time over the last few days, the other Lister generator had not been run since Saturday evening and the inverter batteries were getting very low - about 92V. It was decided to run the generator and give the batteries a good refresh charge. 08:30 3 litres fuel added. Engine started 08:45 Engine producing 115V dc at 30A (3450W) 09:00 Inverter enabled, office supply switched to inverter power, dishwasher started. 09:30 Generator producing 31.5A at 108.6V. (3420W) Inverter drawing 26.7A - dishwasher on heater cycle. 10:40 Dishwasher ends cycle 11:00 Engine shut down. Washing machine started on inverter. Inverter power meter 49.4kWh Run time 150 minutes |
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| Friday 19th October 2007. 18:00 3 litres fuel added. Engine started. 20:00 Engine shut down. |
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| Saturday 20th October 2007. 19:00 4 litres fuel added. Engine started. 19:20 1.7kW storage heater turned on as test load. 21:00 Engine shut down. Today was the big plumbing day. A 4 port manifold was constructed from copper pipe fittings, which would allow the Lister and the boiler to work together and supply heat to the radiators, hot water cylinder and underfloor heating loop. By 7pm the manifold had been installed and it was time to fire up the Lister. Earlier we had had some circulation problems because of air in the circuit. Once this was bled, the system worked fine. At 8pm the temperature of the water into the house was 50 degrees, at 9pm it was 80 degrees. There is sufficient heat available to run another radiator and the hot water tank from the Lister heat. These connections will be added to the manifold later. Hence the 4 isolating valves on the outputs - the unused ones are easily shut off. Next year we are planning to build a 16 m2 conservatory. The underfloor heating loop will be connected in series with the return heat pipe that runs back to the Lister. This will ensure that the last dregs of useful heat are extracted from the hot water, and that the return water temperature to the Lister is as cool as possible - probably around 30 degrees C. |
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| The manifold is soldered using plumber's solder applied to the end-feed fittings. There is a skill required to make successful, neat end feed joints, and even on the bench with a big blowtorch, I found it difficult to keep things neat. However with plenty of flux and a little patience it soon came together and most importantly, it was leak-free. The worst of the flux staining was removed with a pan scrub. |
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| Overview of the manifold. Boiler feeds in from left hand side via a non-return valve. The pumped Lister circuit feeds in from the right hand side through an isolation valve and a non-return valve. Behind the manifold is the modified pipe to feed the flow into the living room radiator which required an angle fitting to be soldered to it. The 15mm isolating valves can be bough in packs of 10 from Wickes for about £1.30 each. I fit them everywhere, it makes later servicing and alterations so much easier to do if you can isolate a section. |
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| Close-up of the four manifold outlets having cleaned off all the soldering flux and discolouration. These will feed 2 radiators, the coil in the hot water cylinder and the underfloor heating loop. |
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| The circulation pump for the Lister was plumbed in, and a 180 degree "loop" arranged to get over some of the awkwardness of dealing with 22mm flexible plastic piping. Isolation valves fitted as standard, but the pump really needs an air bleed screw on its right hand outlet so that the air can be released more easily. Enamelled dish was to catch the drips when it was bled by slackening off the right hand union. Small bore pipes on left of photo were the original pump feeds to the shed. They are redundant now and will be removed. |
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| The manifold is installed under the floorboards in the heating access space. The four branches can just be seen in the foreground. Flexible hoses were ised becaus of the problems of making rigid connections reliably in such a tight space. |
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| The lounge radiator is 900mm wide by 600mm high double convector. It produces about 1500W of heat when at 50C. This photo is just to the right of the fireplace in the living room. It has seen at least 3 generations of heating added, from a primitive back boiler in the 1920s to a modern condensing gas boiler in 2005. All the pipes pass horizontally beneath this access hatch and then vertically up the side of the chimney breast. |
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| I made a 4 branch manifold that would allow either the boiler or the Lister or both, to feed the 4 separate heating circuits. Both the boiler and the Lister are pumped systems, and so at the left and right arm of the manifold is a non-return valve, to stop the water from the Lister shorting through the boiler heat exchanger and vice versa. The 4 outlets from the manifold feed separate circuits, namely lounge radiator, underfloor heating loop, coil in the hot water cylinder and one spare for connecting to additional radiators. I wanted to check that the Lister could run the existing heat load before adding more. In the shed, the Lister thermosyphons into a 120 litre storage tank. It also has an exhaust gas heat exchanger, that feeds into a heating coil in the storage tank. The tank moderates the water temperature from the exhaust heat exchanger and also allows the Lister to run for about 2 hours without any overheating problem. After 1 hour, the water back to the house was coming at 50C. After 2 hours it was 80C. I then shut down the engine and 90 minutes later the water is still returning at 50C - using up the heat from the local store. I'd been planning this job for a long time but finally got around to doing it. I ran the Lister tonight with a 1.7kW storage heater as the load. That heater heats my office whilst the loung is heated by a 1.5kW double convector radiator. The underfloor heating also got nice and warm - it's about 15 square meters in the tiled kitchen and bathroom. It's now 95 minutes since I shut down the engine, and the water from the shed is still coming in at 47.5C. That small store certainly seems to be doing it's job. Boiler hasn't fired since 7pm. I will now probably adapt a solar controller to turn the pump on and off automatically when it senses the exhaust gas heat exchanger getting hot. I still have lots of insulation to do on the ex-gas-H.E., and some improved pipe runs - but basically the system is functional. I will finish the plumbing of the hot water cylinder coil tomorrow and possibly use the spare output of the manifold to drive another radiator or possibly a 200 litre thermal store located in the understairs cupboard.. |
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| Saturday 27th October As I have been busy, I have not been running the engine as much as I would like this week, about every other day. Here is a summary: Saturday 20th October. 4 Litres of fuel added. Engine run time 120 minutes Sunday 20th October. 3 Litres of fuel added. Engine run time 120 minutes Tuesday 22nd October. 3 Litres of fuel added. Engine run time 90 minutes Thursday 24th October. 3 Litres of fuel added. Engine run time 90 minutes Saturday 27th October. 3 Litres of fuel added. Engine run time 230 minutes On Thursday I made a heating element for the high pressure fuel line. It appears to be working well and heating the injected oil up to about 75 degrees C. This has helped reduce the black soot and improved the fuel economy. Saturday was spent erecting the framework for the extension to the engine shed. This will add approximately 2.25m x 3m to the engine shed and give a load more undercover, insulated dry storage space. Unfortunately my PMDC starter/generator failed today during the 4 hour run. It overheated and unfortunately the permanent magnets have been cooked beyond their Curie temperature and lost their permanence. This means that there will be a pause in proceedings until I can get the Startomatic engine fully commissioned with exhaust and cooling systems and up and running. The Lister generator set was reconfigured so as to allow the ST alternator to provide battery charging of the main battery bank and a 1500W UPS used to supply clean power to the office. By the middle of November, another electricity meter had been installed to monitor the power suppled bu the ST alternator and it was time again for a test run and system shakedown. Thursday 15th November 19:30 3 litres of fuel added and engine started. 3kW Furnace used as load 21:00 Engine shut down Runtime 90 minutes Energy supplied 2.79kWh Friday 16th November 18:30 3 litres of fuel added and engine started. 3kW Furnace used as load 21:30 Engine shut down Runtime 180 minutes Energy supplied 5.07 kWh |
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| Thursday 22nd November 18:35 3 litres of fuel added and engine started to charge batteries 22:00 Engine shutdown 205 minutes runtime Friday 23rd November 11:45 3 litres of fuel added and engine started 14:30 3 more litres added 15:30 4 litres added 20:00 Engine shutdown Total of 8 hours 15 minutes. Approximately 10 litres of fuel used. 17.1 kWh recorded on new electricity meter. New watt meter running at 37 pulse per minute (1000 = 1kWh) - about 2.22kW Over the next few days the Lister was run regularly 22/11/2007 3 l oil 205 mins 23/11/2007 10 l oil 495 mins 24/11/2007 6 l oil 330 mins 25/11/2007 9 l oil 275 mins 30/11/2007 3 l oil 230 mins 1/12/2007 9 l oil 466 mins 3/12/2007 7 l oil 332 mins 12/12/2007 6 l oil 105 mins 13/12/2007 30 mins - testing out new pump system 14/12/2007 3l oil 240 mins - further testing of pump in cold return pipe. Total 56 litres 2708 mins During this time 83kWh of electricity was produced. A good friend dropped by with 80 litres of good quality used vegetable oil, so there was now plenty of oil for some extended run periods. On 12th and 13th December the plumbing was altered to remove the 120 litre local store in the shed and to connect the pump immediately before the exhaust gas heat exchanger. The pump managed to push 6 litres per minute around the system. The modifications seemed to work OK and the final temperature of the water from the engine reached a plateau of 65 degrees C after 2 hours of running. After 4 hours run time the water temperature had plateaued out to 67 C -ideal for the radiator and the plastic pipe runs. During this time, the principal loads on the ST alternator were a 1500W PTC room heater and the 1100W battery charger. The meter on the ST output was running at 35 pulses per minute - so approximately 2.1kW load. |
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| Saturday 15th December Now that the pump has been moved to the return pipe to the Lister and the water is being positively pushed through the system, the circulation is now reliable. The pump manages almost exactly 6 litres per minute, and this provides adequate cooling of the Lister without excessive temperatures in the pipework. As measured yesterday, the water entering the house does not quite reach 70 C. This could be improved by insulating the exhaust gas heat exchanger which will reduce its losses significantly - so one of this weekend's jobs is to wrap it in rockwool. Additionally, there are certain improvements to the pipework, which will reduce losses in the piperuns as well as making the system neater and more stable. The primary consideration is adequate cooling of the engine, without over-cooling, and keeping the temperature of the water flow, well within the temperature specification of the plastic pipework. |
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| Today I also experimented with different flow rates - using the 3 settings on the Wilo circulation pump. After 2 hours on the maximum setting, I tried the middle and the lower settings. At 14:47 the flow temperature went dangerously into the 90's which sent me running for the shed to shut the engine down. Of course, this shut off the circulation pump - so I had to plug that into the maintained supply in order to allow things to cool down a little. By 15:02 things were back to normal temperature - so I restarted the engine. I reverted to the original full speed pump, and things seemed to stabilise again at 65 C. Time started 07:58 Time Stopped 14:47 Run time 409 minutes Meter kWh 95.3 kWh Power used 12.3 kWh Engine restarted 15:02 3 l fuel added 17:00 3 litres of fuel were added at 07:55, 10:00, 12:00, 14:00, 17:00, 19:00 and 21:00 making 21 litres in total. Consumption appears to be slightly short of 3 litres every 2 hours - probably 1.35 litres per hour. Whilst there is the desire to run the Lister as hot as possible, you certainly don't want to run the polypipe at temperatures approaching 90C for extended periods of time. Polypipe is rated at 90C at 6 bar of pressure - whilst my system is not pressurised, the 90C is the limiting factor. At 15:30 the temperature had stabilised to 68C, the thermal output was 4.49kW and the engine was producing 2.1kW of electricity. The skies had cleared and outside temperatures were down to 1.5C and dropping fast. Fortunately I had plenty of oil - and the means to keep the house comfortably warm. By mid- afternoon, I bit the bullet and decided to connect up the coil of the hot water cylinder to the Lister heat manifold. A length of 10mm barrier pipe was already very nearly in place - left over from the original solar heating installation. To connect up, I made up an isolating valve on a bit of pipe, and without draining the system, cut into the 15mm pipe and fitted the isolating valve - with almost no loss of water. Then I tee'd the 10mm barrier pipe into this feed, so that it would direct hot water from the Lister into the coil of the cylinder, after the automatic valve, so that the Lister would heat the tank whenever it was running. After checking all the compression joints for weeps, I then released both isolating valves and the hot water began to flow through the coil. I also realised that if I closed the gate valve on the boiler pump, and opened both the automatic valves for the hot-water and central heating, that I could direct the flow of Lister heated hot water around the rest of the radiators in the house. After selectively setting the thermostatic radiator control valves to allow water through, I then went to monitor the flow and return temperatures and the flow rate. 425 litres per hour at a temperature differen | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||